........to load a cartridge!!
I have been waiting on a set of dies for my Schuetzen rifle for I believe 3-4 months and they aren't here.....yet. I have been wanting to work with that rifle and had tried some loads but never got close to what I believe is its potential. In fact the results were abysmal. I remain convinced that was because as yet I had no way to properly size the neck of the formed cases. The die I made is drilled a bit off center and pushes sort of a shoulder on the case when used. Obviously my machine skills could use some improvement....a LOT of improvement. As the mold for the 9.3 X 57 had arrived and I've cast quite a few bullets for it I'm now waiting for them to cure.....which got me to thinking about the Schuetzen rifle while I was at my casting bench.
A sizing die is a sizing die, right? What I mean is if a bullet sizing die is of hardened steel or tool steel as is a sizing and decapping die then they perform the same function whether the material sized is brass or lead, right? All I needed to do with the Schuetzen cartridge case was to neck size it. Soooooo.....as I have several oddball bullet sizing dies if I had one that would take the case neck to the proper diameter and could figure out a way to make my ancient Lyman-Ideal sizer/luber work I could size the case necks to the proper diameter.....right? I dug through my container of sizing dies and found one I thought might work. It is the .372 die for the 9.3 cast bullets. I discovered that by changing the pin that pushes the bullet out of the sizer/luber it would open wide enough to allow the case to enter. A little minor lathe work and a new pin was made then cut to length after trial and error. The .372 die was installed in the sizer/luber, a case neck was lubed with regular case lube, case inserted and made certain it was centered and I "shoved it on home". It came back out with less resistance than a sized bullet.....GREAT!!!! Now to measure the case mouth and check a bullet. Doggone it......still a bit too big. I knew I had a .363 die but feared it might be too tight. Still, that's only .009 which is .0045 a side. I changed dies and "shoved it on home" again. Same two checks, dimensions and with the bullet......hmmmm....this might work.
As I don't have the dies for the .345 caliber rifle and that is.......at best an unusual caliber.....I needed to figure out how to bell the case mouth. I have a really strange set of 38 Spl. dies. The belling die has two calibers on it, one for 38 Spl. then one above it for about 40 cal.....which is a bit big for a .345 bullet. They are the only set of dies I have ever seen that way. I'm game to try about anything to make the rifle shoot accurately at this point so I screwed the 38 Spl. die into the press and put one of the newly neck sized cases in the shellholder, raised it into the die and just barely bumped the handle. I couldn't even see the ram move. Pulled the case out of the die and it had a very slight flare in the case mouth, then I tried a bullet. Son-of-a-gun!!!! This WILL work I believe!!!!!!
I only did 10 cases as there was some doubt and I didn't want hours spent doing something that might not work. I loaded the 10 cases with 20 grains of Reloader 7, seated the bullets then took the bell out of the case mouth by inserting them into my 32-20 taper crimp die. 10 loaded cartridges! Now it was time to see if I was right about the crooked sizing die I had made and if the rifle would shoot somewhat like I thought it should given its excellent bore. Off to my little home range, staple up a new target and settle down at the bench with front rest and butt bag in place. Below is the target. Shots 1 & 2 were completely off the paper high. I dropped the rear sight adjustment quite a bit and returned to the bench. Shot 3 landed in the 6 ring and #4 in the 7. As can be see they're still nothing to talk about at 50 yards, benched and bagged. There was only one thread of elevation adjustment left and I took it then turned in a little right windage and decided to fire the remaining 5 rounds for a real group. They went into a cluster of 1 inch with 4 under 5/8 inch, C to C. I hope the group can be even tighter next time out as I was really fighting the sun on the big eye cup on the aperture sight. I need to crank in just a bit more right windage but that will come later. Oh, I had to make a little wrench for the sight adjustment square headed screws and it is at the bottom in the 6 ring. It started out as a piece of 1 1/2 X 1 1/2 angle iron 3/16 thick. Hand ground and filed and hopefully a little temper given to it!!! The rifle is in the second picture.
I have been waiting on a set of dies for my Schuetzen rifle for I believe 3-4 months and they aren't here.....yet. I have been wanting to work with that rifle and had tried some loads but never got close to what I believe is its potential. In fact the results were abysmal. I remain convinced that was because as yet I had no way to properly size the neck of the formed cases. The die I made is drilled a bit off center and pushes sort of a shoulder on the case when used. Obviously my machine skills could use some improvement....a LOT of improvement. As the mold for the 9.3 X 57 had arrived and I've cast quite a few bullets for it I'm now waiting for them to cure.....which got me to thinking about the Schuetzen rifle while I was at my casting bench.
A sizing die is a sizing die, right? What I mean is if a bullet sizing die is of hardened steel or tool steel as is a sizing and decapping die then they perform the same function whether the material sized is brass or lead, right? All I needed to do with the Schuetzen cartridge case was to neck size it. Soooooo.....as I have several oddball bullet sizing dies if I had one that would take the case neck to the proper diameter and could figure out a way to make my ancient Lyman-Ideal sizer/luber work I could size the case necks to the proper diameter.....right? I dug through my container of sizing dies and found one I thought might work. It is the .372 die for the 9.3 cast bullets. I discovered that by changing the pin that pushes the bullet out of the sizer/luber it would open wide enough to allow the case to enter. A little minor lathe work and a new pin was made then cut to length after trial and error. The .372 die was installed in the sizer/luber, a case neck was lubed with regular case lube, case inserted and made certain it was centered and I "shoved it on home". It came back out with less resistance than a sized bullet.....GREAT!!!! Now to measure the case mouth and check a bullet. Doggone it......still a bit too big. I knew I had a .363 die but feared it might be too tight. Still, that's only .009 which is .0045 a side. I changed dies and "shoved it on home" again. Same two checks, dimensions and with the bullet......hmmmm....this might work.
As I don't have the dies for the .345 caliber rifle and that is.......at best an unusual caliber.....I needed to figure out how to bell the case mouth. I have a really strange set of 38 Spl. dies. The belling die has two calibers on it, one for 38 Spl. then one above it for about 40 cal.....which is a bit big for a .345 bullet. They are the only set of dies I have ever seen that way. I'm game to try about anything to make the rifle shoot accurately at this point so I screwed the 38 Spl. die into the press and put one of the newly neck sized cases in the shellholder, raised it into the die and just barely bumped the handle. I couldn't even see the ram move. Pulled the case out of the die and it had a very slight flare in the case mouth, then I tried a bullet. Son-of-a-gun!!!! This WILL work I believe!!!!!!
I only did 10 cases as there was some doubt and I didn't want hours spent doing something that might not work. I loaded the 10 cases with 20 grains of Reloader 7, seated the bullets then took the bell out of the case mouth by inserting them into my 32-20 taper crimp die. 10 loaded cartridges! Now it was time to see if I was right about the crooked sizing die I had made and if the rifle would shoot somewhat like I thought it should given its excellent bore. Off to my little home range, staple up a new target and settle down at the bench with front rest and butt bag in place. Below is the target. Shots 1 & 2 were completely off the paper high. I dropped the rear sight adjustment quite a bit and returned to the bench. Shot 3 landed in the 6 ring and #4 in the 7. As can be see they're still nothing to talk about at 50 yards, benched and bagged. There was only one thread of elevation adjustment left and I took it then turned in a little right windage and decided to fire the remaining 5 rounds for a real group. They went into a cluster of 1 inch with 4 under 5/8 inch, C to C. I hope the group can be even tighter next time out as I was really fighting the sun on the big eye cup on the aperture sight. I need to crank in just a bit more right windage but that will come later. Oh, I had to make a little wrench for the sight adjustment square headed screws and it is at the bottom in the 6 ring. It started out as a piece of 1 1/2 X 1 1/2 angle iron 3/16 thick. Hand ground and filed and hopefully a little temper given to it!!! The rifle is in the second picture.
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